Sunday, February 10, 2013

Restore IV

The body of the dulcitone was in pretty poor condition, but pretty much intact. A rather nasty hairline crack was remedied by sinking very long thin dowels down the one side to reinforce the frame. All parts that could be removed (such as the lid) were separated from the rest of the body and completely sanded down with cracks and gouges filled and corner chips refashioned with small shards of wood. The body itself was sanded down to remove the years of caked on dust, random swipes of enamel paint, and corroded varnish.



Several runs of aerosol insect killer and turpentine were aimed at all suspicious woodworm holes.

The legs needed to be rebuilt, along with the brackets that attached them with a hinge to the base of the instrument.


Online photos of intact models were used to calculate the approximate dimensions.


The original legs were fastened to the dulcitone base with some rather nifty thumbscrews which also enabled relatively easy release to fold them under the base, allowing for storage or transportation. The small remaining fragment of thumbscrew gave enough away to convince us that screws and threads like this simply did not exist anymore and it would be better to replace them with something brand new that at least functioned in the spirit as the  original.



This took a couple of attempts to get right. Included below are both the first attempts and the final mechanism.

First prototype using wing-nuts



Final version with silver soldered nuts and bolts

Sadly the wing-nut version could not be used as there was not enough clearance for the heads. Oblong threaded washers were sunk into the dulcitone base to complete the mechanism.


Thumbscrews installed

In jobs like these, the jigs you use are often just as important as the finished product. The more time spent making the correct bracket to hold something in place, the more likely you are going to be successful in your endeavors.  We built a number of jigs and purpose made tools to make our lives easier. These included: 
  • a little mounting bracket to place the snapped off tuning forks in order to test the spring steel fork holders we were making, 
  • a little felt tipped hammer to strike the forks to test them when the keyboard was removed, 

  • drill guides in order to sink very long dowels into the dulcitone body for reinforcement 
  • and this simple but effective foam lined bracket that allowed us to turn the whole instrument upside down so as to work on it with out disturbing or otherwise straining any of the delicates.



If this all sounds very time consuming, then consider that we had not even started the french polishing!

EDIT: Parts 1,2,3,5 and 6 of this story

Sunday, February 3, 2013

Restore III

So where to begin? What needed fixing? How did we fix it?

Any replacement parts required were unlikely to be found in some spare parts store, so we either had to find the closest possible alternative or manufacture new parts from scratch. Even something as simple as replacement springs required months of following up leads and multiple candidate spring purchases (small runs of designer springs are too financially prohibitive)  and testing with samples so as not to introduce a more inferior, or too strong spring into the equation. Here is a brief summary of some of the things we worked on to improve or fix the overall mechanism:


a.) 
As one of the white keys had missing ivory on top a suitable replacement in the form of 1 millimetre acrylonitrile butadiene styrene (ABS) plastic was sourced. This was about the same thickness as the ivory and had been recommended by a piano restorer that I had made a few inquiries with. Since the use of ivory for piano keys is basically illegal plastic was the only viable alternative. It could be scored to the dimensions required and then snapped at exactly these cuts to make a very accurate replacement. (although a little whiter than the yellowed original)

(It's the A#)

In addition to this, other, loose ivory was re-glued and the keyboard was cleaned removing years of caked on dust and vermin excrement. A combination of rubbing alcohol swabs and slowly applied amounts of toothpaste appeared to provide the best results. An earlier attempt with nail polish remover proved too corrosive to the shiny finish of the ivory.

b.) 
Finding suitable springs for the back of the keys proved most problematic. This was largely a trial and error process. Given that the keying mechanism does not need to be as sensitive as a piano's, since a player is not really capable of pianissimo type dynamics on the dulcitone, we felt it acceptable to err slightly with springs that were probably stronger than the originals when they were new. This was guesswork as we had no idea what the action of a brand new dulcitone felt like.



c.) 
While a lot of the hammers had felt that certainly showed signs of being snacked upon, they were still in reasonable condition. There was, however, one that had broken right off.


Interpolating the dimensions of the missing hammer by looking at the hammers on either side,


a new core was carved out of teak.

(Notice the slightly elongated base to cater for part of the hammer dowel that was snapped off.)


Felting of piano type hammers involves the use of hydraulic presses capable of exerting 35 tons of pressure in order to pre-shape and glue the felt in low temperature controlled environments. In the absence of this, we sourced 1cm thick dense white felt, cut this to shape and glued it around the teak core with many mini-vices to keep the felt from buckling. A little bit of steam was applied to the felt before hand to make it slightly more pliable.

After assembly, the attack onto the forks was deemed a little 'soft' compared to the other hammers, so a light application of diluted wood glue was applied to the surface which restored some of the 'bite' to the hammer's attack. Job done!


d.) 
When the hammers return to rest after being pressed their dowels are pressed against felt of approximately 4mm thick. Much of this felt had been eaten away by vermin. Replacement felt was relatively easy to source and apply. The only interesting anecdote worth recalling is that to retract all 61 hammers simultaneously away from their resting point in order to glue down the felt strip required a 1cm diameter steel rod. A wooded dowel almost snapped under the combined strength of all the hammer and key springs.   
Another view of the new hammer and the re-felted surface against the dowels

e.)
This area contains an essential part of the keying and hammering mechanism as the hammers trajectory downwards onto the forks is guided by an ingenious combination of springs, felted pads coated with fabric and a simple cam that governs the exact depth of the hammer strike and controls the retraction of the hammer upon striking the forks so at not to strangle the tone. Some of these were in dubious condition and a number of new fabric coated felts were introduced. Each cam surface was given a coating of graphite powder for lubrication. This stage was particularly time consuming, hell on the back and constantly felt like being both on the performing, and receiving end of a root canal!

f.)
Replacement of all felting cushioning the actual keys as they come into contact with the dulcitone body so as to minimize any unwanted percussive noise. This included the manufacturing of circular pieces of felt needing to be placed around the metal rods which govern the key trajectory. 61 times. Each metal rod, sanded of oxidation and grit to ensure smooth key action. 61 times. Yeah.


g.)
Each damper felt was replaced with 5mm felt. A lot if this fine work (not only to remove the felt but also glue) was performed with a high speed Dremel tool using a variety of heads. Its doubtful such non-invasive precision could have been performed with anything else.

The damper mechanism itself is initiated upon release of the keys, when two tiny springs bring the damper gracefully down onto the just-stuck, vibrating forks to deaden all tone. Due to years of over-stretching, these tiny springs, I suspect, had become weakened to the point that not all of them came down with sufficient force to mute the vibrating forks. Sourcing springs tiny enough seemed fruitless. Even if we did find some the mechanism would have been rather difficult to get at to do any micro surgery on.

Instead, we opted to place and glue tiny lead fishing weights just above the felt on each of the problematic dampers. In most cases this provided sufficient moment to successfully choke all vibrating forks.

Two different types of weights depending on the severity of the damper spring so as to not unnecessarily overweight the mechanism.

This fix brought about an additional improvement. With all tuning forks properly dampened in their default or rest position, there were less vibrational noises when playing the instrument which would normally be caused by sympathetic vibration. 

h.)
While all the tuning forks were still present, some were rather badly oxidized  which affected tone, timbre and tuning. Not being able to do too much about tuning, we opted to very, very carefully clean and polish some of the bad ones which considerably improved the tone and sustain when struck.

Tuning bracelets (added for fine tuning adjustment upon installation) had come loose from the forks and were contributing to sundry rattling. these were firmly reattached with blobs of glue.


Photo depicting rusty tuning fork with loose tuning bracelets, missing springs, eaten hammer felt, not retracting hammers and damper felt about to fall off. The wooden piece with the nails in folds over the forks with the nails keeping the forks apart so they don't bash against each other when being transported. 

i.)
A number of the leather fork holders needed to be replaced as the leather itself had hardened or perished to the point where they were providing little support and tension for the forks. This was again a rather laborious process and made harder by the presence of the aforementioned fork tuning bracelets. Suitable screws and paper washers (made from gasket paper material) needed to be sourced and manufactured as there was significant rust and wear to those components.

j.)
The 7 smallest tuning forks had completely snapped off their sheet metal fork lift springs. This was not a trivial salvage job as they were initially riveted onto the forks. Their job was to provide support but also be sufficiently  springy to allow the forks to vibrate freely.

First the old rivets were drilled out, then a machining tap was used to cut an internal thread in the hole of the tuning fork. This would allow a new spring support to be screwed in. This was not easy at all!

Finally, a suitable sheet metal fork lift replacement needed to be sought. Our first thoughts were to use sections from the spiral of a clock spring. This unfortunately did not provide the elasticity to allow the smaller forks to vibrate when stuck. In the end trimmed and shaped sections of sardine can lids provided the solution.

Fresh leather holders as discussed in (i) and forks 1 through 7, from right to left all with their new sardine can fork lift springs.

k.)
All the felt directly below the forks was replaced. This reduced rattling and buzzing significantly.

l.)
The sustain pedal and body of the dulcitone will be discussed in subsequent posts.

EDIT: Parts 1,2,4,5 and 6 of this story

Sunday, January 27, 2013

Restore II

For the uninitiated or the lazy the dulcitone was designed and manufactured in Scotland in the late 19th and early 20th century. By about 1915, production was halted as either popularity waned or impracticality of mass production and portability had the final word. Not being the loudest of acoustic instruments, its characteristic timbre was ultimately better sought by composers and ensemble arrangers in the louder vibraphone or celesta.
Photo: Andreas E Beurmann

What does the instrument sound like? To my ears, a lot like an acoustic version of a Fender Rhodes electric piano with a special warmth in tone somewhat lacking in say, the celesta. Of the 2000 odd manufactured, very few are in existence today and even less in passable working order. I suspect that this something to do with the rather bold claim that they were "portable", with fold-able legs allowing for transportation but rather delicate innards to be entirely suited to the rigors of the missionary's ox wagon.

Those delicate innards are best described with the aid of the following diagram courtesy of Sue Mo from her informative website.


In short, a hammering system, not unlike that of a grand piano, was employed to disengage a damper and strike a steel u-shaped tuning fork (which was responsible for the beautiful bell-like tone) which was held in place by oblong leather pieces. These maintained sufficient tension on the forks which rest on u-shaped sheet metal springs.I have made one minor alteration to Sue's diagram above in blue. There is additional felt that may or may not come into contact with some of the tuning forks (certainly some of the larger heavier ones) and this seems to ensure that there is minimal rattle when they are struck by the hammers. As can be seen from the diagram above, a rather intricate series of felted surfaces, springs and even a simple cam work in concert to enable the whole mechanism to work perfectly and noiselessly.

A foot operated pedal can be used to disengage damping entirely allow for more sustain when playing.

EDIT: Parts 1,3,4,5 and 6 of this story

Monday, January 21, 2013

Restore

I am looking through an old EXCEL spreadsheet I found on my laptop from when we first opened this thing up after I got it back from the junk shop that masqueraded as an antique shop. I had decided to make some notes about what was broken and what needed fixing.

On a musical instrument with 61 piano-style keys, a lot can not work. A total of 18 keys made no sound at all. That's a success rate of about 70%. Does that sound like a passing mark? The average chord and melody when playing a keyboard requires about 4 keys to work concurrently, so the chances are, that you would play a harmonically weakened chord or strike a horrible empty phantom note in your melody.

I'll admit that when I describe it like that it almost sounds intriguing, but playing a keyboard note in vain has to rank as one of the most soul sapping sensations imaginable. Of those 40 odd keys that produced a chime, very few produced a pleasant consistent, repeatable tone and few had a damping mechanism that worked at all. Looking at the filthy baby coffin sized box, it all seemed like a bit of a lost cause - a lost cause that I was sure I had been over charged for.

It's not like I could shop around for a better deal. At about one hundred years old, and relegated from all but the most niche musical ensembles, if you find an old dulcitone, you buy it.
If these probing torch lit photographs resemble some recently uncovered sunken treasure then you are not far off. There was a sense of a long undisturbed and very brittle find about the whole affair and early forays and views of the structure were beset with some trepidation of making a rather sorry situation a lot worse.

There was a lot of oxidation, desiccated leather, felt consumed by vermin, overstretched springs, missing or broken key components, evidence of wood worm infestation and about a century of caked on dust and cockroach poop. 

This was going to be a real task.

EDIT: Parts 2,3,4,5 and 6 of this story

Sunday, January 13, 2013

Nostalghia

Been looking for a clearer, cleaner version of this for years.

and some information to boot

Thank you internet!

Lifted directly from description body of second video)


Oh,kumushki*, be friends with each other 
Be friends with each other and love each other
And love me too
Go to green garden
And take me with you 
You'll gather flowers
Gather some for me too
You'll wreathe chaplets
Oh,wreathe one for me too

Go to the Danube river
And take me with you 
You'll sail your chaplets by water
And sail mine too
Your chaplets were sailing adrift
But mine has sunk...swam like a stone..swam like a stone
Your sweethearts have returned from war
But mine hasn't 
He doesn't come back, he doesn't write any letters
He's forgot about me...about me... 

* 'Kumushki' means lady friends, particularly those, who have exchanged their baptismal crosses for a week, in accordance with the old Russian custom,done soon after Easter Sunday

Friday, June 29, 2012

Saturday, May 26, 2012

John Jacob Niles

 John Jacob Niles - Go 'Way From My Window



John Jacob Niles - The Murdered Brother



John Jacob Niles - The Hangman